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次镜调整机构如图1所示,包括次镜组件(实现次镜支撑及其自由度约束)、调焦传动组件(实现高精度柔性铰链传动)以及直线传动组件(作为次镜调整机构输入,输出精密直线运动)。
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次镜调整机构的基本原理如图2所示,调整机构左右完全对称且具备主备份调焦能力,结构上包含次镜及导向铰链、柔性传动机构、主(备)份直线驱动器以及倾斜盘等几个部分。主(备)份直线传动组件具备优于2 μm分辨率精密致动能力,假如A点向图2所示的下方运动1 μm,B点会以P为支点向上运动0.2 μm (AP和BP长度比例为5∶1),从而带动“倾斜盘”以D为支点顺时针旋转,进而对称面上H点柔性变形片向上运动且位移量为C点的1/2,从而驱动次镜发生0.1 μm的精密轴向运动。
即次镜调整机构将直线传动组件的直线输出通过柔性铰链的变形转换为调焦传动组件顶端的“倾斜盘”运动,从而驱动次镜组件的高精度移动。次镜调整机构具有以下特点。
(1)驱动机构冗余设计:驱动电机是调整机构设计的关键,采取驱动机构冗余设计以保证可靠性,主(备)份电机中的任何一个正常工作均可保证调整机构功能及性能;
(2)采用柔性铰链传动:相比传统的齿轮减速具有冲击小、无磨损、传动平稳、可靠性高的优点,同时柔性铰链在微小位移范围的传动中具有较高的精度;
(3)柔性导向铰链:通过柔性导向铰链的设计,使次镜及其组件在光轴方向具有一定柔性,而在其他方向上刚度较强,保证调焦过程中次镜的倾斜以及偏心在一定的误差范围内。
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次镜调整机构从步进电机输出旋转运动到次镜的高精度移动共经过三个环节减速,其中包含一次旋转运动到直线运动的转换,传动比分配如下。
环节一:步进电机配合行星齿轮减速器,减速比iA=112.89∶1;
环节二:切口螺母旋转转换为螺纹传动导杆的直线运动,螺纹导程S=1.0 mm;
环节三:柔性传动铰链构成减速比10∶1的差分减速杠杆,减速比iB=10∶1。
步进电机步距角γ=1.8°,按上述传动关系,理论上次镜沿轴向的移动分辨率d按照公式(1)给出:
$$ {d}=(\gamma / 360^{\circ}) \times( { 1/i_A }) \times S \times(1 / i_B) $$ (1) 计算可知分辨率d为4.4 nm,次镜的移动步距取决于步进电机的控制,在轨调焦一般按照每128/64/32步作为一个最小控制量,对应的次镜移动分辨率为128d/64d/32d = 0.56 μm/0.28 μm/0.14 μm。
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图3为次镜组件示意图,包括具有较高比刚度的蜂窝夹芯式ULE次镜及支撑背板、Bipod杆以及柔性导向铰链等。
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采用步进减速电机作为动力,如图4所示。通过滑动螺旋传动实现旋转运动转化为直线输出,具有结构紧凑、运转平稳、易于自锁的特点,通过预紧弹簧进行消间隙控制以确保传动精度和稳定性。
常用的螺旋传动包括滑动螺旋传动以及滚动螺旋传动,二者的对比如表1所示。
表 1 常用的螺旋传动对比
Table 1. Comparison of common screw drives
Sliding spiral drive Rolling screw drive Advantages Simple structure and low cost; Easy to self-lock Low friction and high transmission efficiency;
No additional clearance elimination design requiredDisadvantages High friction and low transmission efficiency; Clearance elimination
design is requiredComplex structure and high cost; Need anti reversal design -
调焦传动组件是基于柔性变形原理设计的铰链传动机构,可以实现图2所示的调焦功能,传动铰链具备10∶1的传动比,为左右对称式构型。
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次镜组件通过三处周向均布的柔性铰链实现次镜的精密导向,柔性铰链使次镜在沿光轴方向具有一定柔性的同时,限制次镜其他自由度。
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调焦过程中为了探测次镜在调整机构工作时所处的绝对位置,直线传动组件末端采用直线差分传感器LVDT(Linear Variable Differential Transformer)反馈直线传动组件末端直线运动的绝对位置,构建闭环控制系统,如图5所示。
次镜调焦过程中,直线差分传感器组件中的差分传感器输入轴、差分传感器输出轴在差分传感器内腔滑动,通过数据采集设备即可测量得到直线传动组件的位置,差分传感器输出轴的位移等价于图2中A点(主份)或E点(备份)的绝对位置变化量,由于柔性传动铰链是设计状态为减速比10∶1的差分减速杠杆,因此闭环控制时可直接通过差分传感器输出轴除以10得到次镜的位移。
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空间防冷焊的方式包括运动副选用不同的材料、固体润滑以及油脂润滑等形式。次镜组件采用柔性铰链释放沿光轴方向的自由度,调焦传动组件通过柔性铰链的变形传递运动,无需采用防冷焊措施。对于直线致动组件涉及的步进电机、行星齿轮减速器涉及的轴承和齿轮副均采用表面镀覆MoS2固体润滑薄膜层防止冷焊效应的发生。
滑动螺旋副采用切口螺母与螺纹导杆配合的形式,选用青铜与超硬不锈钢两种不同的配合材料,啮合段表面涂覆真空润滑脂进行防冷焊,通过调节切口螺母外预紧环实现螺纹消隙,如图6所示。
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该套精密调整机构在完成力学试验后开展了调整精度试验,试验按照步进减速电机每次转0.088°(对应的次镜理论步距8.858 μm)进行调整,次镜的初始位置为零位,驱动次镜依次完成“零位、正极限位置、零位、负极限位置、零位”整个调整循环。
如图7所示,调整机构精度测试时次镜调整机构放置于三坐标平台,光轴竖直向上。首先通过三坐标采集次镜三杆上三处周向120°均布的共面凸台建立测量基准,然后采集次镜在每次调整步距下的外圆柱拟合圆心的平移变化,用于表征次镜偏心量。通过采集次镜背部平面与测量基准面之间距离及法线的变化计算次镜的绝对位置和倾斜量。
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如图8所示,实测次镜的调整行程为+128.6~134.6 μm,结果满足≥±120 μm调整范围的要求,其中横坐标为步进减速电机的调整步数,纵坐标为次镜的绝对位置。
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如图9所示,横坐标为次镜的绝对位置,纵坐标为次镜在各位置的倾斜。次镜在整个调整行程内的倾斜偏差总均方根最大值为1.93″,满足总体要求的在调整行程内倾斜小于3″的要求。
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如图10所示,横坐标为次镜的绝对位置,纵坐标为次镜在各位置的偏心量。可以看出次镜偏心量的总均方根最大值为1.33 μm,满足总体要求小于5 μm的要求。
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如图11所示,横坐标为完成“零位、正极限位置、零位、负极限位置、零位”整个调整循环对应的步进减速电机调整步数,纵坐标为每次调整对应的次镜实测步距。可以看出,实测调整步距达到设计预期。
次镜调整机构的步距精度(3σ值)按公式(2)给出,定义为每次实测步距相对于标定步距的偏差,取多次测量的标准偏差RMS的3倍。实测次镜步距为8.732 μm,步距精度ASn (3σ)为0.18 μm。
$$ A{S_n} = \sqrt {\dfrac{{\displaystyle\sum\limits_{i = 1}^n {{{({d_n} - {S_n} \times n)}^2}} }}{{n - 1}}} \times 3 $$ (2) 式中:Sn为标定步距,即通过测量得出的平均步距;i为调节次数;n为调节单位;ASn为调焦步距精度3σ值;dn为调节一个n单位时的实测调节距离。
Design and test of precision secondary mirror adjustment mechanism for space optical remote sensor
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摘要: 随着空间光学遥感器地面分辨率逐步提高,长焦距、大口径相机成为重点研究方向。为了克服重力变化、复合材料变形等因素带来的天地不一致性的问题,次镜调整成为校正光学遥感器离焦和主次镜相对位置变化的关键技术之一。将次镜柔性支撑、精密直线驱动与柔性铰链传动技术相结合,设计了一套高精度次镜调整机构。首先介绍了该套机构的光机构成、工作原理及传动链路,然后对超轻次镜、高精度直线致动、高精度调焦传动等设计分别进行了阐述,最后介绍了力学环境试验后的调整精度测试情况。试验结果表明,该套精密调整机构实测调整行程大于±120 μm,轴向调整步距精度0.18 μm (3σ值),调整行程内次镜的最大平移误差为1.30 μm,最大倾斜误差为1.93″,具有调整范围宽、调整精度高的特点,满足空间光学遥感器精密次镜调整的要求,已成功在轨应用于北京三号B卫星0.5 m级高分辨率空间相机。Abstract:
Objective Vertical assembly and adjustment is one of the key technologies of long focal length and large aperture space camera. In order to overcome the inconsistency between the on-orbit and the ground caused by gravity change, material deformation and other factors, the secondary mirror adjustment has become one of the key technologies to correct the defocus of the optical remote sensor and the relative position change of the primary mirror and the secondary mirror. Precision secondary mirror adjustment technology has been widely used in high-resolution space optical remote sensors. For example, Stewart platform 6-DOF parallel mechanism, which has been successfully applied in Hubble telescope and reconnaissance camera, has the advantages of high accuracy, high bearing capacity and high rigidity, and has the ability to precisely adjust the secondary mirror components in the optical system. Many theoretical analysis and engineering research have been done on the 6-DOF adjustment mechanism in China, but the 6-DOF adjustment mechanism also has the disadvantages of complex structure and control system, high cost and relatively large weight. Therefore, it is necessary to develop a single-degree-of-freedom secondary mirror adjustment mechanism with high accuracy, high integration and high reliability to solve the inconsistency between heaven and earth faced by the current high-resolution space optical remote sensor. Methods In order to meet the secondary mirror adjustment requirements of a high-resolution camera, a high-precision and high-stability secondary mirror adjustment mechanism combining precision linear transmission, flexible transmission and flexible support technology is built in this paper (Fig.1). The linear transmission device (Fig.4) adopts the redundancy design of one main and one standby, and has precision position telemetry capability. The flexible transmission hinge with transmission ratio of 10∶1 is used for motion transmission. Compared with the traditional gear reducer, it has the advantages of small impact, no wear, stable transmission, and high reliability. At the same time, the flexible hinge has the advantages of high-precision transmission in the range of small displacement. The secondary mirror uses bipod flexible support to design unloading force thermal deformation, and ensures its flexibility along the optical axis direction (focusing direction) through three pairs of 120° flexible guide hinges. Results and Discussions This set of precision adjustment mechanism has carried out adjustment precision test after completing the mechanical environment assessment. The test is carried out according to 0.088° rotation of step motor (corresponding theoretical step distance of secondary mirror 8.858 μm). The initial position of the secondary mirror is zero. The secondary mirror is drived to complete the whole adjustment cycle of "zero position→positive limit position→zero position→negative limit position→zero position". The adjustment accuracy test results after the mechanical environment assessment of the optical and mechanical products of the adjustment mechanism show that the mechanism has the ability to achieve high-precision adjustment in a large range (Fig.8-11), and meets the requirements of the on-orbit application of space optical remote sensor. Conclusions In this paper, a set of high-precision secondary mirror adjustment mechanism is designed by combining the flexible support, precision linear drive and flexible hinge transmission technology of the second mirror. This paper first introduces the optical and mechanical structure, working principle and transmission link of the mechanism, then describes the design of ultra-light secondary mirror assembly, high-precision linear actuation and high-precision focusing transmission, and finally introduces the adjustment accuracy test after the vibration test. The test results show that the measured adjustment stroke of the set of precision adjustment mechanism is more than ±120 μm, the axial adjustment step precision is 0.18 μm, the maximum translation error of the secondary mirror within the adjustment stroke is 1.3 μm, and the maximum tilt error is 1.9″. It has the characteristics of wide adjustment range and high adjustment accuracy, and meets the requirements of the precision secondary mirror adjustment of the space optical remote sensor. -
Key words:
- large aperture /
- space optics /
- adjustment mechanism /
- remote sensor /
- secondary mirror /
- flexible support
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表 1 常用的螺旋传动对比
Table 1. Comparison of common screw drives
Sliding spiral drive Rolling screw drive Advantages Simple structure and low cost; Easy to self-lock Low friction and high transmission efficiency;
No additional clearance elimination design requiredDisadvantages High friction and low transmission efficiency; Clearance elimination
design is requiredComplex structure and high cost; Need anti reversal design -
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